CASE STUDY: PILOT PLANT FOR NITRATE REMOVAL IN GROUNDWATER - - PowerPoint PPT Presentation

case study pilot plant for nitrate removal in groundwater
SMART_READER_LITE
LIVE PREVIEW

CASE STUDY: PILOT PLANT FOR NITRATE REMOVAL IN GROUNDWATER - - PowerPoint PPT Presentation

CASE STUDY: PILOT PLANT FOR NITRATE REMOVAL IN GROUNDWATER USING ION EXCHANGE AND BIOPHYSICAL TREATMENT OF THE RECIRCULATING REGENERANT S. Tarre, M. Beliavski, M. Green Faculty of Civil and Environmental Engineering Technion Israel


slide-1
SLIDE 1
  • S. Tarre, M. Beliavski, M. Green

Faculty of Civil and Environmental Engineering Technion – Israel Institute of Technology Haifa, Israel

CASE STUDY: PILOT PLANT FOR NITRATE REMOVAL IN GROUNDWATER USING ION EXCHANGE AND BIOPHYSICAL TREATMENT OF THE RECIRCULATING REGENERANT

SWWS ‐ Sept. 2016

slide-2
SLIDE 2
  • In Israel, about 250 wells are closed = 80,000,000 m3/yr

The Problem:

  • Well size = 25 – 100 m3/hr
  • In Israel, high nitrate concentrations in groundwater is

the main reason for closing wells in the coastal aquifer.

slide-3
SLIDE 3
  • The technologies for nitrate removal fall into two

categories: physico‐chemical processes and biological processes

  • Physico‐chemical processes (ion exchange, R.O.,

electrodialysis) were the preferred method. Main problem is the brine produced ‐ difficult to treat and dispose

Options for Nitrate Removal from Groundwater:

  • Biological process (denitrification). Disadvantages are

the intensive post‐treatment required and stringent health regulations.

slide-4
SLIDE 4

Proposed Solution :

Combined ion exchange and bio‐regeneration process

  • Nitrate is separated from the water by Ion

Exchange (IX).

  • Exhausted IX column is regenerated by brine

solution recycling with a denitrifying reactor Advantages:

  • Almost zero brine and wastewater discharge
  • Separation of the biological treatment from the

water supply

slide-5
SLIDE 5

Combined System Scheme:

Adsorption phase

Raw water Product water

Regeneration phase

NO3 Selective IX resin

IX

NO3 rich brine NO3 free brine Waste brine disposal Biological denitrification (NO3 ‐> N2) + Post‐ treatment

slide-6
SLIDE 6

Process Objectives: First investigated by Van der Hoek and Klapwijk, 1987; Clifford and Liu, 1993, 1996

Combined Concept is not ‘new’:

Still not implemented on at full scale. Combined process problems:

  • Relatively complicated vs other processes
  • Poor quality of recycling regenerant brine: high DOC, high SS

requiring frequent replacement , resin contamination

  • Still ion exchange, high chloride addition to product water and

wastewater from resin washing  Minimize chloride addition to water supply  Improve recycling brine quality for extended use  Minimize brine production  Minimize IX column bacterial contamination

slide-7
SLIDE 7

Ion exchange columns – to adsorb nitrate from water Sequential Batch Reactor – to remove nitrate from brine

Pilot Plant Combined System Components:

Ozonation – for brine polishing and recycling

slide-8
SLIDE 8
slide-9
SLIDE 9
slide-10
SLIDE 10
slide-11
SLIDE 11
slide-12
SLIDE 12
slide-13
SLIDE 13
  • Minimize Cl‐exchange for NO3

‐ to 1:1, however

  • Water also contains HCO3

‐ and SO4 2‐ ions that can be

exchanged, significantly increasing product water Cl‐

  • The solution is to use a “Nitrate Selective” IX resin and

extend length of ion exchange service cycle till column breakthrough

Minimizing Chloride Addition During Ion Exchange:

slide-14
SLIDE 14

Raw and IX Product Water Composition

5 10 15 20 25 30 50 100 150 200 250 300 350 400 Raw Water 160 BV 380 BV 480 BV N-NO3 SO4-S Cl N-NO3 and S-SO4 mg/L Cl mg/L

slide-15
SLIDE 15

Raw and IX Product Water Composition

5 10 15 20 25 30 50 100 150 200 250 300 350 400 Raw Water 160 BV 380 BV 480 BV N-NO3 SO4-S Cl N-NO3 and S-SO4 mg/L Cl mg/L

slide-16
SLIDE 16

Brine Denitrification: Improving SBR Effluent Quality

  • Ethanol was used as the electron donor
  • Ethanol dosage critical for SBR effluent quality
  • The solution was to supply the necessary amount of

ethanol by sequential dosing and ORP monitoring and control

  • HCl added to maintain pH~8.2 and Cl‐compensation
slide-17
SLIDE 17

SBR Control

50 100 150

  • 400
  • 300
  • 200
  • 100

100 1 2 3 4 5 6 7 8 N-NO3 mg/L ORP mV Time (hours) 65% % EtOH dosage

slide-18
SLIDE 18

SBR Control

50 100 150

  • 400
  • 300
  • 200
  • 100

100 1 2 3 4 5 6 7 8 N-NO3 N-NO2 mg/L ORP mV Time (hours) 65% % EtOH dosage

slide-19
SLIDE 19

SBR Control

50 100 150

  • 400
  • 300
  • 200
  • 100

100 1 2 3 4 5 6 7 8 N-NO3 N-NO2 ORP(mV) mg/L ORP mV Time (hours) 65% % EtOH dosage 10% 10% 10% 5%

slide-20
SLIDE 20
  • Near 100% suspended solids removal
  • SBR effluent has high turbidity, poor filterability and

high bacterial counts.

  • DOC of 40 mg/l requiring IX column disinfection
  • Minimal waste production due to foam

formation and separation

  • High turbidity reduction from 30 NTU to 1~3

Improving Poor SBR Effluent Quality (con’t)

The solution was Ozonation for sustainable regenerant recycling

slide-21
SLIDE 21

5 10 15 20 25 30 35 40 30 60 90 120 150 Turbidity - NTU Time - Min Ozone Treatment of SBR Effluent

slide-22
SLIDE 22

Minimization of waste brine for removal:

Sources of waste brine and wastewater in the system

IX columns flush of H2O2 Disinfectant; EC=1.1 0.96 BV Sewage Disinfection Waste 1st fill; EC=28 0.66 BV Truck Disinfection Drain 2nd fill; EC=1.4 0.89 BV Sewage Regenerant Waste; EC=57 0.28 BV Truck

0.4% wastewater 0.2% waste brine

slide-23
SLIDE 23

Tzur Moshe Pilot Summary:

  • Chloride increased from 84 to 121 mg/L
  • Nitrate was reduced from 95 to 31 mg/L as NO3

  • No increase in product DOC; low bacterial counts
  • Competitive price $0.35/m3
  • Pilot Plant operated for 1 yr; regenerant not replaced
  • 99.4% water recovery
slide-24
SLIDE 24

Thank you!