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geothermal reservoir conclusions from case study Gross Schoenebeck - - PowerPoint PPT Presentation

Drilling a geothermal well into a deep sedimentary geothermal reservoir conclusions from case study Gross Schoenebeck Wulf Brandt & Geothermics Group GeoForschungsZentrum Potsdam In situ Geothermal Laboratory Baltic Sea DB Kobenhavn


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SLIDE 1

Drilling a geothermal well into a deep sedimentary geothermal reservoir – conclusions from case study Gross Schoenebeck

Wulf Brandt & Geothermics Group GeoForschungsZentrum Potsdam

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SLIDE 2

In situ Geothermal Laboratory

Paris Bruxelles London Munich Praha Warszawa Berlin Hamburg Kobenhavn

NEGB PT NWGB NEB DB

North Sea Baltic Sea

Rotliegend Tornquist zone Variszican belt Variszican Deformation front Caledonian Deformation front Caledonides &

  • lder massifs

Precambrian crystalline basement Alps

Rhenohercynian Saxothuringian Moldanubian A l p i n e front 100 200 km

Gross Schoenebeck

(modified after Ziegler 1990, Bertelsen 1992, Brecht 1999)

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SLIDE 3

Operations overview

  • pen hole proppant frac

Jan/Feb 2002  production test / logging  4130-4190m (frac 1)  4080-4118m (frac 2)  production test / logging

  • pen hole waterfrac

start Jan/Feb 2003  3874-4294m, borehole instability  production test

  • cont. Nov/Dec 2003

 4135-4309m  production test / logging Dec 2004  injection test April 2006 to Jan 2007  drilling 2. well

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SLIDE 4

0n the way to an operating doublet well path of second well

  • designed as deviated well
  • in direction of minimum horizontal stress
  • to optimize performance of doublet

aim

  • maximization of flow rate
  • for 30 years
  • avoid thermal short circuit

scheduled fracture treatments

  • designed to achieve PI > 30 m³/(h*MPa)
  • sufficient for geothermal power production
  • n economic level
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SLIDE 5

EGS Gross Schoenebeck

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SLIDE 6

Borehole Design of the Research Well

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SLIDE 7

Lessons learned

  • drilling a large diameter borehole in sheet

silicate bearing rocks (sequenzes of sand/sandstones and clay/mudstones)

  • directional drilling through and beneath rock

salt formations with plastic behaviour

  • Adaptation to encountered geological

conditions requires the variability of mud concepts with the goal of minimized formation damage

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SLIDE 8

Large top hole diameter affected ROP

Insufficient pumping capacity in the top hole region (23“) lead to bit balling resulting in a ROP of 4…7 m/h and an increased number of trips. Improper bit selection reduced ROP in the mesozoic section (16“).

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SLIDE 9

disastrous cementation of 16“x13 3/8“ casing

Total fluid loss occured during the cementation of the combined casing 16“ x 13 3/8“ despite of a slurry density of 1450 kg/m³ (Litefil by Schlumberger) due to plugging of the annulus by debris

temperature logs

40 50 60 70 80 90 100 500 1000 1500 2000 2500 depth [m]

  • temp. [°C]

temperature while caliper logging before casing running temperature effects of remained cement setting in caverns cement losses into Muschelkalk temperature after cementation probable top of solid cement

Conclusion:

Free pipe will not stand the thermally induced stresses to be expected (buckling). Free floating pipe is not acceptable.

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SLIDE 10

Recovery of casing cementation

To prevent casing damage in the future of the production well a reverse squeeze cementation through the annulus was designed and successfully performed:

temperature logs squeeze cementation

45 50 55 60 65 70 75 80 85 700 800 900 1000 1100 1200 1300 1400 1500 1600 depth [m] temperature [°C]

  • 6
  • 4
  • 2

2 4 6 8 10 temperature differences [K] 22.9.06 before Frac 23.9.06 after Frac 23.9.06 before Cementing 24.9.06 after Cementing DT vor/nach Frac DT vor/nach Zem DT vor Frac bis nach Zem.

Obviously no annular flow

1. Free point estimation and cement bond log verified top

  • f cement

2. Fluid loss during injection

  • ccurs near to

top of cement 3. Slurry density

  • f squeeze

cement with 1,30 below density of mud to be displaced

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SLIDE 11

Well design concepts for deep geothermal wells

HDR Soultz fully cemented production casing partly cemented production casing suspended protective casing free moving suspended at well head inside of polished bore receptable

Pro´s

successful cementing very likely no dislocation within the casing string low costs prevention of circulation behind the casing cost savings no buckling no tensile loads at the wellhead

Con´s

buckling unavoidable complete cement column must be secured annular circulation possible very high tensional load required for avoiding buckling

  • nly applicable in solid rocks

with no breakouts to be expected any fluid flow behind the uncemented casing must strictly be excluded no thermally induced forces acting on the production string non-suspended free floating production casing tightness problems possible due to casing motion EGS Groß Schoenebeck resp. geothermal wells in sediments

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SLIDE 12

Casing collapse within the rock salt

9 5/8“ liner collapsed during drilling into the target formation after reduction of mud density from 2000 kg/m³ to 1060 kg/m³ (Heavy deformation between 3880…3200 m)

Ovality 8 mm

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SLIDE 13

Cause of collapse Casing design – according to the rules with an overburden pressure gradient of 2,3 Casing material – successfully inspected Anisotropic tension due to well path geometry – unlikely according to cross-correlation Anisotropic tension due to rock salt inhomogenities within the salt dome in connection with the geomechanical impact of drilling – not verifiable Anisotropic tension due to improper cementation of the deviated well – not very probable due to no. and positioning of centralizers and cementing procedure strictly following the simulation

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SLIDE 14

Remedy for the collaps

The loss of one casing dimension forced to adjust the borehole design – drilling of the Rotliegend section with 5 7/8“ and running and cementing of an combined 5“ liner with an uncemented section of preperforated pipes on bottom.

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SLIDE 15

Conclusions

Cost effective drilling of geothermal wells means Considering all costs emerging over the lifetime

  • f the well

Design the well as tall as possible but leave one ace upon your sleeve With highly corrosive fluids provide demountable coated or lined production/injection strings Particularly to geothermal producers and injectors adapted repair technologies for casings should be available

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SLIDE 16

Tubingless insert ESP minimizes well diameter Is the geothermal „industry“ strong enough to demand such developments?

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Repair of cemented casings Means and technologies of expandables are to be worked

  • ut and assessed in

cooperation with experienced players:  Cladded liners (casing patch)  Downhole coating of casing  Downhole relining of casing with thin (folded) metallic liners Reasons

  • Internal corrosion due to air access during production/injection
  • Closing of perforations etc. (e.g. after secondary cementing)