Aluminium & Power, Jharsuguda
BEST PRACTICES ON ENERGY SAVINGS SESA STERLITE LTD JHARSUGUDA , - - PowerPoint PPT Presentation
BEST PRACTICES ON ENERGY SAVINGS SESA STERLITE LTD JHARSUGUDA , - - PowerPoint PPT Presentation
Aluminium & Power, Jharsuguda BEST PRACTICES ON ENERGY SAVINGS SESA STERLITE LTD JHARSUGUDA , ODISHA Aluminium & Power, Jharsuguda GROUP PHILOSOPHY Our Mission Our Values Excellence Our mission is to be a Growth world-class
Aluminium & Power, Jharsuguda
GROUP PHILOSOPHY
Humble Smart Hungry Our DNA Our Vision “We will be the world’s most admired company that consistently defines the leading standards in our businesses, making
- ur
stakeholders proud to be associated with us.” Our Values Our Mission “Our mission is to be a world-class metals and mining group and generate superior financial returns.”
Growth Trust Sustainability Excellence Entrepreneurship 4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
BUSINESS DIVERSIFIED
→ Sesa Sterlite, a Vedanta Group company is one of the world‘ largest global diversified natural resource company. → FTSE 100 London Stock Exchange listed company. → Operations span across India, Sri Lanka, Africa, South Africa, Europe and Australia.
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
PLANT LOCATION
INDIA
PLANT SITE 4/29/2015 KEP WORKSHOP
ODISHA
Aluminium & Power, Jharsuguda
PLANT PROFILE
Capacity of 3615 MW ISO 9001,14001,50001 & OHSAS 18001 Certified Water Source – Hirakud Reservoir Coal Source- Mahanadi Coal Fields High Concentration Slurry Disposal Hybrid ESP with SPM level < 40mg/Nm3
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
IMPLEMENTATION & LEARNINGS ISO 50001 ENERGY MANAGEMENT SYSTEMS
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
ENERGY MANAGEMENT TEAM- POWER
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
CPP : Kick-off ISO 50001:2011 30th Jan 2012 Stage-2 Audit (Certification Audit) 12th - 15th Sept 2012 IPP : Kick off ISO 50001:2011 30th Jun 2012 Certification Audit 26th Feb 2013 to 1st Mar 2013
MILESTONES ISO 50001
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
ENCON EFFORTS & BENEFITS
Implementation of Total Quality Mngt. Culture Implementation of New Technologies Implementation of IT Enablement in procuring Energy Efficient Equipments Improvement in Process & Operational Practices Development and Implementation of Innovative and Breakthrough Energy Efficiency Improvement Projects. Daily Monitoring of Specific Consumptions & Deviation Analysis Energy Improvement Projects is linked to Individual KRA’s Energy Audit by CII in June’11 & ISO 50001 implementation & certification in the year of 2012
SHR = 2442 Kcal/kwh ; APC= 9.66%; SOC = 0.11 ml/kwh
2014-15
2010-11 SHR = 2678 Kcal ; APC= 10.14%; SOC= 0.80ml/kwh
4/29/2015 KEP WORKSHOP
SHR = 2337 Kcal/kwh; APC= 8.08%; SOC= 0.38 ml/kwh IPP CPP SHR= 2430 Kcal/kwh; APC= 9.89%; SOC= 1.12 ml/kwh IPP CPP 2012-13
Aluminium & Power, Jharsuguda
- 1. Selective Soot-blowing:
- Optimized need based soot-blowing resulting in flue gas exhaust temperature from
141°C to 137°C and reduction in super-heater spray by 2% that is 8 T/hrs.
- Annual saving- 5.82 MTOE
- 2. Stoppage of purging of HFO guns:
- Purging of HFO guns on regular basis are stopped
- Annual saving- 35.93 MTOE
- 3. Optimization of key Process Parameters:
- Operational optimization by maintaining the technical parameters like Main-steam
pressure, main-steam temperature , etc. near to design value.
- Annual saving- 3.17 MTOE
PROCESS IMPROVEMENT (9X135 MW)
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
- 6. Optimized running of Dry Ash conveying system:
- Running of Dry-Ash conveying system in level mode from timer mode resulting in
stoppage of 1 compressor.
- Annual saving- 188.31 MTOE
- 5. Optimized use of Compressor:
- Stoppage of Dryers in Service Air system (6 nos.)
- Arresting of leakages and rectification of intake valve passing resulting in stoppage
- f 1 compressor.
- Annual saving- 188.31 MTOE
- 4. Cooling Tower fan door plugging:
- Plugging of the holes of Cooling Tower fans, hence reduction in fan loading via
excess air leakage and improvement in vacuum.
- Annual saving- 22.14 MTOE
4/29/2015 KEP WORKSHOP
PROCESS IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- 7. Optimization in Electrostatic Precipitator :
- The 1st Field ESP hopper heaters are switched off during normal running of the
units.
- Each hopper consist of 2 heaters of 3Kw each.
- Annual saving- 72.31 MTOE
- 8. Improvement in Belt utilization:
- Improvement in Belt utilization by rectifying the track hopper, ILMS (In-line
magnetic separator and replacement of existing conveyor with the new conveyor.
- Annual saving- 65.34 MTOE
- 9. Operational Optimization of Mills Lube-Oil pump:
- Stoppage of stand-by Mills Lube-Oil pump
- Annual saving- 45.19 MTOE
4/29/2015 KEP WORKSHOP
PROCESS IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
PROCESS IMPROVEMENT (4X600 MW)
4/29/2015 KEP WORKSHOP
- 1. Increase Reheater temp(528°C to 538°C):
- Daily Monitoring HRD sheet
- SADC checking(S/D)
- Burner tilt operation
- Increase in HRH temp from 528 to 538°C
- Unit heat rate improved by 2 kcal/kwh
- Annual saving- 1653 MTOE
- 2. Identification and plugging of air ingress points in flue gas ducts
- Flue gas, air duct leakage detection resulting in ID FAN Avg. current reduced from 246 A to
234 A. (power reduce by 0.5 MW) &.083 % APC reduction
- Annual saving- 376 MTOE
- 3. PA Fan power reduction by arresting air leakage
- Seal air leakage detection and PA hot air and cold air to mill leakage detection in U#2
resulting in PA FAN A- Current reduced from 106 A to 86 A and PA FAN B-108 A to 82 A (Power reduced by 0.95 MW) APC reduced by 0.158 %.
- Annual saving- 715 MTOE
Aluminium & Power, Jharsuguda
4/29/2015 KEP WORKSHOP
- 4. Optimization of idle running hours of drives:
- Stopping of One CW pump as per circulating water inlet and outlet
temperature.
- Annual Saving: 393 MTOE/Unit
- Stopping of one Vacuum pump as per condenser Vacuum
- Annual Saving : 216 MTOE/Unit
- Stopping of DP pump for makeup in condenser.
- Annual Saving - 203 MTOE/Unit
- Implementation of shutdown checklist to Stop the running equipment
- Annual Saving - 144 MTOE/Unit
- During Unit Startup use TDBFP instead of MDBFP
- Annual Saving - 120 MTOE/Unit
- Stopping of 1 seal air fan(250 kw) by arresting seal air leakages
- Annual Saving: 41 MTOE/Unit
PROCESS IMPROVEMENT (4X600 MW)
Aluminium & Power, Jharsuguda
4/29/2015 KEP WORKSHOP
- 5. Reduction of start up time:
- Six Sigma project implemented to reduce very hot startup
- Step by step activity/process prepared
- Very hot startup time reduced to 1hr 35min to 1hr 10min
- saving- 63 MTOE
1.60 1.16
0.00 0.50 1.00 1.50 before after
Very hot Start up
PROCESS IMPROVEMENT (4X600 MW)
- 6. Reduction of startup time by Deaerator pegging in boiler and turbine preheating
- Boiler feed water temp increased to 121°C (earlier 50°C) by deaerator pegging. Which
raised the furnace temp to 97°C (earlier temp was 40°C).Time reduced to 20 min
- During turbine preheating ,HP inner /outer casing temp was raised to 204 /192° C instead
- f 150°C ,which has reduced the time of heat soak by 2 hrs.
- SAVING : reduction in oil consumption during startup to 121 MTOE
Reduction in time by heat soaking
4.5 2.5 1 2 3 4 5 before after 2.29 1.52 1 2 3 before after
Reduction in time by increasing furnace temp
Aluminium & Power, Jharsuguda
4/29/2015 KEP WORKSHOP
8.Reducing the output voltage of lighting transformer
- No of taps were reduced in lighting transformer with a reduction in voltage from 432 volts to
415 volts resulted in power saving of 30.2 Kwhr per day
- Annual Saving: 1 MTOE
9.Increasing ash utilization by disposing Ash through trucks
- Reduction of ash conveying from transfer silo to terminal silo, as D-pump ash conveying
capacity averagely 260tns/hr. Stopped one compressor.
- Geho pump dispose 260T of ash per hour. As 4,500T of ash transported through trucks,
per month 18 hours of Geho running hour reduced.
- Saving of 10654 kwhr power per month and specific power: 0.05 Kwhr/MT
- Annual saving: 7 MTOE
PROCESS IMPROVEMENT (4X600 MW)
- 7. Reduction of Number of Trips :
- Identify the root cause of all unit outages
- Implement recommendation of Trip analysis
- saving- 150 MTOE/Unit
Aluminium & Power, Jharsuguda
4/29/2015 KEP WORKSHOP
10.Increasing CHP conveyor belt utilization
- Increasing coal conveyor belt utilization from 50 % to 60 % (from 1500 TPH to 1980 TPH)
to minimize the power consumption with saving of 922 MWhr
- Annual Saving:97 MTOE
- 11. Reduction of Rake Turn Around Time
- Elimination of idle running time of stream and compressor with a saving of 263 MWhr
- Annual Saving: 22 MTOE
PROCESS IMPROVEMENT (4X600 MW)
Aluminium & Power, Jharsuguda
- 1. Condenser Cleaning (Jet, bullet & chemical):
- Condenser Jet cleaning=1 unit; Bullet cleaning=4 Units; Chemical cleaning=1 unit
- Average improvement of 20 kCal/kWh/Unit/Kpa in Heat Rate.
- Annual saving- 148.74 MTOE
BEFORE AFTER
TECHNOLOGY IMPROVEMENT (9X135 MW)
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
- 2. Air Preheater seal and basket replacement :
- Air Preheater Baskets and soft touch seals replaced resulting in Improvement of
boiler efficiency by 0.5%
- Reduction in Primary Air Fan (PA) loading of 103 Kwh
- Annual Saving: 620.50 MTOE
BEFORE AFTER
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- 3. CT Fans Blades Replacement :
- For each unit, 5 CT cells are designed.
- Weight of GRP blades is more than FRP blades.
- Total 13 nos. of GRP blades replaced with FRP blades.
- Average Savings : 234.70 MTOE.
BEFORE AFTER
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- 4. Replacement of Old Chrome rollers with New
Sinter Cast Rollers & Liners
- Rollers & Liners are replaced by New Sinter
Cast Rollers
- Reduction in Mill power consumption by 30 KW.
- Running hours increased from 6000 to 18000
hrs.
- Savings : 17.54 MTOE.
BEFORE
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- 5. CW pump Impeller coating:
- CW pump impellers coated with
Brush able coating
- Reduction in CW pump loading
by 68 kw
- Annual Saving: 45.19 MTOE.
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- 6. Ultrafilteration Installation to Reduce DM Water Consumption:
- Installation of Ultrafiltration System to reduce the colloidal silica in
Demineralized (DM) water.
- Reduction of Blow down losses by 80% & heat losses.
- Annual Saving: Rs. 213.62 Million.
Ultra-filtration System
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- 7. Modification of Fly Ash Conveying System:
- Due to modification the consumption of compressed service air reduced
resulting in stoppage of 2 compressors.
- Each of the units was provided with a separate air vessel to compensate the
fluctuations.
- The ash collection vessel size was increased for ESP 3rd field and same was
placed in 4th field
- Annual Savings: 376.61 MTOE
BEFORE AFTER
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
- Earlier Turbine hall & compressors house consisted of 72 & 16 electrics fans
respectively.
- Each fan rated capacity 3 kw.
- Electric fans are replaced by Eco ventilators (224+28) in TG Hall as well as in
Compressor house.
- Energy savings : 199.39 MTOE
- 8. Installation of Eco Ventilators :
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
Project : Utilization of Waste Water :Effluent Treatment Plant - 2 (ETP) Commissioning. Before:
- More than 4000m3/day of waste
water was discharged out of the plant
- Specific water consumption was
high After:
- Waste water management by
treatment in ETP
- Zero discharge of water out of
plant
- Specific water consumption is
reduced
CPP Synergy Office CPP Switchyard CW Pump Area CT Fans Area
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
Project : ESP Bag Filter Retrofitting.
Before:
- Designed ESP had 5 fields
- Ammonia dozing was in process
- Avg. SPM was more than 100
mg/Nm3 After:
- Last 2 fields replaced with Bag filter
- Ammonia dozing stopped
- Existing Ash Conveying system is
modified
- Avg. SPM < 30mg/Nm3
BEFORE AFTER BEFORE
4/29/2015 KEP WORKSHOP
TECHNOLOGY IMPROVEMENT (9X135 MW)
Aluminium & Power, Jharsuguda
TECHNOLOGY IMPROVEMENT (4X600 MW)
AFTER BEFORE
4/29/2015 KEP WORKSHOP
- 3. Reduction of power in CEP after removal of one stage
- Removal of CEP stage in order to compensate energy loss due to throttling of deaerator
level control valve resulting in CEP Pump-Current reduced from 123A to 92 A. (0.45 MW power reduced & 0.075 % APC
- Annual saving- 167 MTOE
- 1. Boiler Modification(LTSH,ECO,RH):
- Reduced the surface are of LTSH tubes and increase the contact area of economizer
bank which resulted in SH spray reduction and increase in feed water temp.
- The modification includes
- LTRH zone curtailment by 120 tubes
- Installation of riffled tubes over exposed furnace water wall tubes
- LTSH tube curtailment by 1 bank
- Economizer zone extension by 1bank.
- Annual saving- 4745 MTOE
- 2. Power reduction in CW pump due to speed reduction
- Addition of no of rotor poles from 16 to 18 in CW pump in U#4 for speed reduction saving-
0.233 % APC CWP current reduced from 290 AMPS to 235 AMPS and 1.4 MW saving in power consumption
- Annual Saving: 520 MTOE
Aluminium & Power, Jharsuguda
AFTER BEFORE
4/29/2015 KEP WORKSHOP
- 6. VFD installation in BA slurry pump
- Installation of variable frequency drive in bottom ash slurry pump in U#1,U#2 with a saving
- f 68 Kwhr
- Annual Saving: 45 MTOE
Before After
RPM 990 700-750 KW 135.5 67.3 KVA 160.1 68.4 KWH 3313 1152 KVAH 3881 1168
TECHNOLOGY IMPROVEMENT (4X600 MW)
- 7. Indigenization of ID fan motor
- U#1 ID FAN 1A motor replaced with CGL make with a net saving per day with a new motor
@ 60kw. In addition to this there is a saving due to stoppage of 1 cooling fan having power consumption 7.5 kw and one lube oil pump having power consumption 1.1 kw
- Annual Saving: 9 MTOE
Aluminium & Power, Jharsuguda
AFTER BEFORE
4/29/2015 KEP WORKSHOP
9.Use of induction lamp in mill coal feeder
- Incandescent lamp of 40 w were replaced by induction lamp of 18 Watt in all mill coal
feeders of U#1,U#2 and U#3 with a saving of 528 Kwhr per feeder per day
- Annual Saving: 1 MTOE
TECHNOLOGY IMPROVEMENT (4X600 MW)
- 8. Implementation of auto timer in lighting system
- Earlier for lighting there is no time limit .We have installed timer for illumination in different
area with a saving of 62 kwhr
- Annual Saving: 1.95 MTOE
10.Installation of EPIC-3 controller in ESP field
- In U#2 ESP field controller from Dalian Chinese make to EPIC-3 controller with a flexibility
- f changing field charge ratio resulted in saving of 240 kwhr per day
- Annual Saving: 1 MTOE
Aluminium & Power, Jharsuguda
AFTER BEFORE
4/29/2015 KEP WORKSHOP
- 11. Mill Hot air gate modification and mill lube oil system modification :
- Mill Hot air gate modification and mill lube oil system modification in all 4 units resulting in
reduction of oil consumption by increasing equipment availability which is equivalent to decrease in SOC by 0.2 ml/Kwhr
- Annual saving- 159 MTOE
Mill HAG Modification Mill Lub oil system modification
TECHNOLOGY IMPROVEMENT (4X600 MW)
Aluminium & Power, Jharsuguda
DAILY MONITORING
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
DAILY MONITORING
Monitoring system
- Integrated Energy Meters are installed for HT &
LT motors and configured in DCS. Meters used for all measurements are calibrated as per ISO Standards
- Related Process parameter are displayed on
the DCS screen.
- All relevant energy data is captured from these
resources at regular intervals by PDHR data.
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
TQM CULTURE
5S Certified
- 5S structure, zones created & effective audit is in place.
- 5S Awareness sessions are conducted for direct & indirect
employees
- 6 zones and 24 Subzones
- Total employee engagement in 5S is 128 direct & 450
indirect Quality Circle/ Lean Quality Circles
- Awareness training completed for 360 employees
(SSL & Service provider)
- Total 20 QC teams formed Including SSL employee
and Service providers
- Total 140 SSL employees and service providers are
engaged in this initiative Sig Sigma
- Wave-3 has 9 top priority projects driven by 55 employees
- 4 Team Leaders qualify for Black Belt Certification and 24
Team Members would qualify for Yellow Belt Certification. 4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
Total Savings: 13077 MTOE
Total Savings: 13077 MTOE CPP : 2482.82 MTOE IPP : 10595 MTOE
ENCON SUMMARY IN 3 YEARS
4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
AWARDS & RECOGNITION
7th India Power Award 2014 Engineering Excellence Awards 2014 Excellent Energy Efficient Unit 2014 Top Plant Award -2014 4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
AWARDS & RECOGNITION
6th India Power Award 2013 Engineering Excellence Awards 2013 Excellent Energy Efficient Unit 2013 National Energy Conservation Award-2012 National Energy Conservation Award-2011 4/29/2015 KEP WORKSHOP
Aluminium & Power, Jharsuguda
THANK YOU
4/29/2015 KEP WORKSHOP